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Nyoomies KME R4.1

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@comradef191 comradef191 released this 29 Feb 22:04
· 28 commits to main since this release

MINOR RELEASE

Back when I first started work on this project, it was suggested to me to add a pulldown to the STEP pin of each motor.
Due to this not causing any issues, I never changed it.
Upon releasing R4, i was poked about this, and yep, turns out EN is supposed to have a pullup!

All this revision does is change the resistor inside each stepper socket to connect to the EN pin.
No BoM or config changes are necessary.